The spring semester is already ending, and I’ll do my best
to cover all that I can. Between the OSU Rocketry Team, my senior capstone
project, side projects, following SpaceX, and finishing undergrad work, it has
been the best semester of college yet.
Our senior capstone counterparts doing Speedfest laughed at our methods because they have vacuum sealed components, entire labs, and unlimited resources at their disposal. Not to mention we did all of this in our team member’s garage because we had no place on campus to do this. It shows just how accommodating our department is to the success of our team representing OSU on the national level against 9 other universities in a collegiate rocketry competition. But that’s a whole other topic I could rant about.
This final semester of my undergraduate coursework consisted
of only two classes: my senior design (capstone) course and an aerospace
laboratory that has some parallels to the capstone course. Only 7 credit hours
has been bliss, and while it is just as busy as taking 15 credit hours’ worth
of professional school classes, 90% of my time and work is towards rockets, and
I couldn’t be more excited about it.
My senior design project was with 9 others, some mechanical engineering
majors, some aerospace engineering majors. Most of us were active on the OSU
Rocketry Team, and we worked towards winning the 2018 Argonia Cup. We called
ourselves the OSU Rocket Squad, a nod towards the quad(copter) we developed to
fly aboard our rocket.
The objective of the competition was to take a golf ball
payload to 8000 feet and recover it as closely to the launch site as possible. The
first 3 weeks of the semester involved choosing the best means to recover the
golf ball, whether it be a deployable glider, deployable quadcopter, integrated
glider, integrated quadcopter, or just basic dual deployment recovery via
parachute. The integrated options posed a lot of problems about returning a
20lb+ vehicle from the sky, so those were eliminated early. We chose a
deployable quadcopter for its active stabilization, powered flight, and prior team
member experience. The quadcopter would be the rocket’s nosecone and contain
spring-loaded arms, folding propeller blades, GPS, its own flight computers, a
backup recovery system, remote control override, and of course, a golf ball.
The nosecone and quadcopter structure were made from 3D printed PLA plastics,
and the nose was only 5 inches long. While the nose was short, it contained
internal shelves that housed the electronics, making every cubic centimeter
count.
Our team was split into 3 groups: Structures, Avionics, and
Integration. Structures (my team) focused on building our own fiberglass tubes
that would become our airframe, couplers, and motor mount tubes, and our own fiberglass
sheets that were CNC cut to yield fins, centering rings, bulkplates, and
quadcopter motor mount supports. By using fiberglass cloth, fiberglass resin,
and a casting mandrel, we built countless tubes of varying lengths and
diameters that would have cost over $1000, had we purchased all the parts
commercially. Even with R&D and some failed parts, we estimate that we
spent less than $500 on materials.
Avionics focused on the design, programming, and electronics
needed to make a quad from scratch. Integration designed spring-loaded arms and
worked closely with Avionics to build the functional quad.
In February, our Structures team flew a small rocket made
entirely of our own fiberglass parts on an I357T as a test to ensure it could
withstand all stages of flight including launch, ejection, and landing. It
performed beautifully, and because the tacky fiberglass resin got stuck to
Chad’s garage floor, tabletop, our hands, forearms, arm hair, and shoe soles,
the rocket was appropriately named Everything
Is Sticky.
Chad Kenkel, Gerald McCullers, and myself (Structures Team) |
On the structures side of things, our tubes were then verified
to withstand flight stresses. We worked with a 5” steel pipe that was the only
suitable 5” OD tube on the entire internet long enough and could be purchased
in a single quantity. There were plenty of cardboard mailing tubes that would
have worked, but we would have had to purchase a dozen of them for over $150.
This steel pipe ended up being $50 and worked great for us.
We eventually nailed down a system called the “Pour and Pet”
method for wrapping fiberglass cloth around the mandrel, pouring fiberglass
resin between the layers, and petting it with nitrile gloves on to evenly spread
it. To make tubes from start to finish we needed the mandrel, fiberglass cloth,
fiberglass resin and hardener, red Solo cups for scientific resin measurement,
popsicle stir sticks, butcher paper for wrapping around the mandrel, scissors
to cut parts to size, nitrile gloves, petroleum jelly, and vegetable oil for
lubrication. For making sheets, the process was similar but with 8-12 squares
of cloth precut and put down with resin between each by means of the “Slather
and Scrape” method. Patent pending, of course.
Our senior capstone counterparts doing Speedfest laughed at our methods because they have vacuum sealed components, entire labs, and unlimited resources at their disposal. Not to mention we did all of this in our team member’s garage because we had no place on campus to do this. It shows just how accommodating our department is to the success of our team representing OSU on the national level against 9 other universities in a collegiate rocketry competition. But that’s a whole other topic I could rant about.
We all diligently worked in our respective subteams,
overcoming one challenge and moving on to the next. In March, we flew again
with the Kloudbusters in Argonia, KS, this time a full-scale configuration
using the same motor we expected to use in competition. On the structural side
of things, we made good use of lubricants to aid in removing the tubes from the
casting mandrels, and this rocket was affectionately named Everything Is Slippery. It became our backup rocket in case the
final iteration was damaged prior to flight in any way, and this flight
verified that we would reach the necessary altitude. This launch also tested a
basic version of our quad: the 3D printed structure and a backup recovery
system. This backup system contained a small parachute that would catch the
quad in the event that all systems went offline.
The launch also featured the worst possible wind conditions,
so if the flight went well, we knew that we could fly in the worst-case weather
conditions. Most of the day was spent resolving issues with the quad, and the
generosity of the Kloudbusters and their electrical power supply helped. We
finally launched with 15 minutes remaining in the day’s waiver, and it took off
without a hitch. The up part was great, but a tighter-than expected fit of the
quad inside the airframe prevented the quad from separating at apogee, and
therefore, the drogue also didn’t come out. A ballistic descent wasn’t good,
but fortunately the main parachute caught the rocket and threw the quad away
from the rocket. We recovered the rocket to find no damage whatsoever which was
a huge step regarding the validity of making our own fiberglass components. The
quad took a while to find (it got thrown far away), and it didn’t fare well.
The SLA-printed nosecone and body were smashed to smithereens, and there really
wasn’t much else to see.
Awaiting the altimeter to reach flight-ready status |
Caleb Ritchie, Chad Kenkel, me, and Nick Foster |
What was left of the quad |
It was a day with mixed results, but the fact that the
rocket held up to the extreme jerk of a main-only deployment event was a big
step forward. It was one less thing to worry about, and since that part is what
I was responsible for, I felt relieved, as did my fellow structures team members.
Spring break followed shortly after this launch and that
consisted of ejection charge tests to get the piston working and attempting to
fly the quad. On the quad side of things, 3D printed parts kept breaking, it
couldn’t stabilize, rotor motors malfunctioned and burned out; there were all
kinds of problems. By the end of that week, we couldn’t fly the quad anymore if
we tried because we had to wait on more components to arrive in the mail.
Following spring break, our structures team got back to work
building the tubes and sheets we needed to assemble a second iteration of the
competition rocket. For some unknown reason, our lubrication methods were not
working, and we went to extreme measures to attempt to pull off the tubes. One
of these measures included drilling small holes in the fiberglass tube to tie a
harness of paracord through and then attach those loops to the hitch of an F350
diesel truck. The pipe was tied to a telephone pole, and then the truck slowly
drove forward. The truck engine began to whine and then the paracord ripped
clear through 3 inches of fiberglass. To remove these failed tubes, we heated
the fiberglass with a heat gun and used a screwdriver to chisel all the way
through it and along the tube’s length to cut it off the mandrel. I began
talking to the Speedfest teams to see what options there may be using expensive
wax and release methods. Before we went through with that, we tried just adding
a second wrap of butcher paper, and while the tubes weren’t as clean (seams and
small bulges were present), these could be removed from the mandrel with a
gentle pull. It was frustrating to have wasted over a week on three failed
tubes (including $50 worth of cloth and resin), but this method is now
fool-proof. We even perfected the butcher paper wraps to minimize the seams and
overlaps. This method of an extra wrap of wax paper and petroleum jelly worked
even better than a $50+ wax and release method would have that the Speedfest
people would have done.
Now that we had new tubes again, I began building the
competition version of the rocket, identical in dimensions to the previous, but
more soundly built because I had additional time. With this new rocket, we also
used new fiberglass cloth that we purchased (rather than use that from the
sailing club), that made the tubes much heavier but even more stout. The 40”
aft section that weighed 33 ounces on the last rocket now weighed 54 ounces
with the same number of resin and wraps. Fortunately, we were so far above our
required altitude of 8,000 feet, that the additional weight wasn’t of concern
to us.
Throughout this entire semester, my roommate’s woodshop
tools came in very handy. We were able to use his table saw to cut the fuzzy
and ragged edges off our tubes and sheets, and his new CNC machine was put to
good use. Prior to April, he did all the cuts for us, but during spring break,
he showed me how to operate everything, so I could do all the cuts myself. When
cutting our fins, I added some flair by engraving the OSU logo into the
fiberglass. It was a clean touch that cut into our altitude but looked neat. One
of our team members has a friend who makes vinyl wraps for automobiles and
such, so he got this rocket wrapped for us. It was cleaner and more durable
than any paint job would be.
The rocket was named The
Other Things, inspired by John F. Kennedy’s “We choose to go to the moon”
speech when he says, “We choose to go to the Moon! We choose to go to the Moon in this decade and do the other things, not because they are easy, but because they are hard.” It pairs nicely with our quad which was named The Eagle because it would return to us to complete its mission. The Other Things was completed a week before launch and allowed for ejection charge testing.
The day before launch, we prepared to ejection charge test
all of our rockets flying over the weekend. This included our capstone rocket,
the rocket built by the rocketry team, and our 12’ tall rocket for the
Spaceport America Cup (more on this later). Delays kept us from doing these
tests any earlier, but Friday morning on April 6th, our team congregated at my
house for testing in the backyard. Delays kept us from testing anything until
the late afternoon, and after a few attempts, we got the club’s rocket and the
SA Cup rocket to separate properly. The capstone rocket took so long because new
carbon fiber arms arrived that morning, and it look four hours to get them cut
and fitted properly. Once we finally ejection charge tested it, the brand-new
carbon fiber arms broke on impact with the ground. Turns out, the cheap PVC
works better, so we re-configured the quad with those. We still had issues with
our piston pushing out both the quad and drogue parachute, and we ran out of
ideas on how to fix it. This was baffling because we got it to work over spring
break, but now the night before the launch, we were unsuccessful.
At this point it is 9:00 in the evening, and my roommate
wanted to have the house back (I’d had the team over all afternoon and
evening), so we regrouped at another team member’s apartment to do some final
testing and get it right. A nasty cold front moved in throughout the day, so we
were working outside in freezing temperatures with 20+ mile per hour winds. At
midnight, we finally achieved a partial success, but on the final test, several
rivets holding parts of the quad together sheared through their 3D-printed
holes because the force of ejection was so great. This posed a bigger problem
because we had to secure these parts of the quad back together. Fortunately,
some sheet metal and machine screws did the trick. Amidst all of this, an idea came
to me to get both the quad and drogue to come out properly and that was by
means of an apogee delay on our secondary altimeter. The primary altimeter
would fire at apogee to separate the quad, then the secondary altimeter would
first 3 seconds after apogee and release the drogue parachute. I felt like a
genius, except I wish that idea had come to me weeks ago.
We get everything packed and ready to go at the lab at 2:30
in the morning the day of the launch. I went to Wal-Mart to buy snacks and hand
warmers for the weekend. I managed to find handwarmers only at the
self-checkout isle, the very last place in the store I happened to be. I bought
all 5 packs there.
Once my personal gear was all packed away at home, I got to
bed at 4:00 to sleep for 90 minutes. Funny enough, that was the exact same
amount of sleep I got last year the night before the Argonia Cup. We left
Stillwater just before 7:00 in brutally cold conditions, but with clear skies.
Saturday was relatively uneventful. I assembled the L1500T
motor for our capstone and packed the recovery for that rocket and the SA Cup
test flight. Delays with the quad kept us from flying our capstone rocket that
day. The club flew their entry for the Argonia Cup but because the team’s
recovery lead attached the main parachute too far down the length of the shock
cord, the parachute never exited the tube and the rocket came down hard. Two
fins fractured and could be repaired, but it would take an evening’s worth of
work in Stillwater to fix and fly again. The entire day there hadn’t been a
single qualifying flight by any other team, so as long as we could get up to
altitude and land safely, we had a good shot of winning.
With that, we called it a day and hoped for better success
on Sunday. Many of us wanted to camp out, but only four of us ended up staying
the night on the Rocket Pasture. I may have been able to help out with the
evening’s work, but the 11 hours of sleep I got in my warm sleeping bad was
bliss.
Sunday was a bit warmer, but also windier. We worked first
to get the SA Cup rocket in the air. After a lot of delays with recovery and
loose coupler sections, Results May Vary
took off at 12:30 on an M1500G. Other than an altimeter being programmed to
deploy main at 1200m instead of 1200ft, the flight was flawless. It did also go
1500ft lower than predicted, and we are still investigating that. In the grand
scheme of things, this was the most important flight of the weekend. It
validated our own fiberglass parts and that joining many sections together
wouldn’t be an issue. It was the first successful M flight for the team, and
without a doubt the largest rocket flown in school history. At the Spaceport
America Cup this summer, it will weigh over 60 pounds, carry 360° video, utilize a PID
control-looped airbrake, and reach 10,000ft.
Cowboy Rocketworks with Results May Vary on the pad |
Under M1500G boost |
Once Results May Vary
was recovered, we could go on get the two Argonia Cup entries in the air. Additional
delays persisted, and the weather worsened a bit. Our capstone rocket, The Other Things took off at 2:30 in the
afternoon and the rocket part went without a hitch, from launch to touchdown. The
quad wasn’t big enough to be spotted for a while, but a minute after launch, we
start to see a tiny black dot far above our heads. Our quad created a buzz
among the other teams and spectators, and I think they were as excited as we
were to see whether this would work or not. As this dot grows larger, we start
to see a quad-like shape to it, and everyone starts losing their minds. Bear in
mind, no one has ever accomplished a rocket-launch autonomous drone before that
we are aware of. What was concerning, however, was that our ground control
station that received information from the quad had no kind of telemetry or
data whatsoever. This meant that our 7lb drone had no remote control and with
its long battery life could go rogue, and nothing we could do could stop it.
Once the drone gets within a few hundred feet, we see it is all white, has no
spring-loaded arms, and is carrying a GoPro. That’s when it hits all of us: that isn’t our quad. That was the most
screwed-over I’ve ever felt in my entire life. Apparently, some guy who spent
the whole weekend in his car with an FPV headset on was the pilot of that
drone, and he claimed to have no control over it when it landed in front of
everyone. I call bullshit, and I can only laugh now that someone actually did
that to us when he knew we were all expecting a quad to land there after that
rocket launched.
The OSU Rocket Squad prior to launch |
The Other Things under an L1500T boost |
Anyway, I go out with a couple others to retrieve the rocket
which was completely intact and flew to 8,500ft. The rest of our team found
what was left of the quad after that, and to this day, we’re still trying to
figure out what happened. Not that we were surprised it failed, but it didn’t
look as though it completely fell from 8,500ft either.
The remains of The Eagle |
While we were out recovering, the rocketry team flew again
on a second L1000W. It too came down hard but was in good enough condition to
be a qualified flight. They landed closer than the only other qualifying flight
that day, so OSU Cowboy RocketWorks became back to back Argonia Cup champions!
Our capstone team did have one other flight. A 54mm
minimum-diameter rocket called If You’re
Reading This, It’s Over that was purely for a backup. On a J90W, it chuffed
and spiraled upwards into the clouds in the last 5 minutes of the weekend’s
launch window. The radio tracker suddenly went silent, and I figured it
lawn-darted. An hour later we found it thanks to a feeble signal from the
tracker, and it was buried up to its fins in soil. Even if it had landed
safely, I don’t think it would have reached the necessary altitude to qualify.
As the rocketry team gathered with the trophy for the
picture, I stood with most of my capstone team, and we talked about the
semester’s work, discoveries, failures, and takeaways. It was hard to not have
anything fruitful to show for our efforts, but that’s sometimes how it goes.
Our Avionics team talked about how we truly pushed the limitations of software
and control algorithms to make the quad turn on and fly.
The rocketry team received $1000 cash, another $400 TeleMega
altimeter, and two EasyMini altimeters (each team won one upon registration,
and they are keeping our capstone team’s). I was grateful for that, and it
gives us even more cushion for our expenses at the SA Cup this summer.
As per tradition, we ate at the Taco Bell in Wellington, but
we took our time before leaving. All of us were in deep conversation either
about this semester’s work, what the team could do next year, and how to
proceed with the rest of 2018. Back in Stillwater, we cleaned up the DML and I
was home around midnight. It was a long weekend and not the outcome I was
hoping for, but it was unbelievable how much we learned and were able to take
away from the last 3 months of work. Our discoveries will help the capstone
team next year and our structures work made huge strides for the rocketry team,
as this greatly reduces our reliance on commercial composites.
Since the competition ended, it has been a completely
different couple of weeks. I’ve had abundant free time, time to go to the gym
again, be outside, sleep plenty, and recap our efforts through this senior
design project. We met with our advisors 2 days after the competition, and we
are making a display poster, writing an internal paper to document everything
we did and why, we’ll do a simple rocket launch demonstration flight at
Speedfest (on Everything Is Sticky,
our first test rocket), and after Speedfest, well lift the quad and forward
rocket body via drone, drop the assembly, then eject the quad out and attempt
to fly it down from there. There are fewer variables at play, and we hope we
can get that to work. But as far as rocket-launching the drone, that part is
done.
That is about it in terms of the Argonia Cup, and our senior
capstone project. Because we are still writing about our work, and we have some
minor tasks to still complete, we don’t have a truly “finished” feeling, but that
is alright. This part comes easily because we’ve already done the work; now we
just have to write it down. I’ve been told there are already 7+ juniors who are
interested in doing this capstone project next year, and design ideas are
already being tossed around. A fear of mine was that if we failed this year, it
wouldn’t have been worth the financial investment from our professors, and
they’d discontinue it next year because of our lack of success. There are
certainly other capstone projects that involve just writing a paper which is
significantly cheaper, but nowhere near as exciting. I hope to see OSU has 2 or
more teams registered for next year.
Outside of the capstone project, there has been lots else
going on with rocketry, both OSU-wide and with me personally. I’ll talk about
those in a separate post. I’ll share that one first, so this post appears
first. Thank you for reading, and I look forward to writing here more often
throughout the summer.
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